1993-09-10 Feasibility Studies Water/Sanitary Sewer ImprovementsMEYER-ROHLIN, INC.
ENGINEERS-LAND SURVEYORS 1111 Hwy. 25 N., Buffalo, Minn.55313 Phone 612- 682-1781
September 10, 1993
City of Albertville
c/o Lirda Houghton, Clerk
Box 131
Albertville, MN 55301
RE: Feasibility Studies for I-94 Watermain Crossing
and for Water and Sewer along the Frontage Road
north of I-94
Honorable Mayor and City Council:
As requested, we have-completed the Feasibility Studies for the
water and sanitary sewer improvements for the above-referenced
projects.
PROJECT LGCATION
The I-94.watermain crossing would be located under I-94, just
north ~f Main Street where ari exis~ing 21-inch casing was
previously placed prior to the highway being constructed.
k~atermain and sanitary sewer would be placed along the service
road north of I-94, from the intersection with CSAH 37 to the end
of the service road between Mud Lake and School Lake. The project
would be located in the North Half of Section 1, Township 120,
Range 24, Wright County, Minnesota. See Attachment 1.
I-94 WATERMAIN CRGSSING
Prior to I-94 being ccnstructed, the City placed a 21-inch
Thore P. Meyer, Professional Engineer Robert Rohlin, Licensed Land Surveyor
i
reinforced concrete pipe across the I-94 right-of-way. This was
intended to eventually be used as a casing pipe for a watermain
which would service the area north of the Interstate.
Normally the casing pipe should be six to ten inches larger than
' the carrier pipe. This allows room for the bells on the ends of
i
each section of pipe. Skids are attached to the carrier pipe so
that it can slide into the casing more easily during installation.
These also take up some of the area of the casing.
If the existing casing was in good condition, the maximum size
ductile iron carrier pipe that could be installed would most
likely be a 12-inch pipe. The existing casing is not in good
condition, however. It was apparently damaged from highway
construction.
The casing pipe has been exposed, cleaned out, and elevation and
alignment shots taken at approximately 6-foot to 8-foot intervals
through the 260 feet of casing length. A drawing of the pipe has
been plotted at a large scale and templates of various size pipes
superimposed upon the casing pipe alignment. It would appear that
a 10-inch ductile or PVC may be possible, however questionable, or
an 8"inch ductile iron or PVC pipe, being rigid pipes with very
limited flexibility at the joints, would be the maximum size that
could be installed.
We have explored the use of a polyethylene pipe, which has just
recently been approved by AWWA and Minnesota Health Department for
use in watermain installation. A request would need to be made to
Joint Powers Water for their approval. Polyethylene pipe is a
fusion jointed, relatively flexible pipe, which would eliminate
the extra diameter for the hubs at the joints and also give some
flexibility to follow the misalignments and displacements of the
existing casing pipe.
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T'r.e following table is a comparison of pressure losses through 300
feet of various pipes and sizes for the carrier installation,
using a fire flow of 2,500 gpm.
Pressure
1
Loss/300' Comments
Ductile Iron CL. 52
12" (12.46 I.D.) 2.48 psi size too large
10" (10.40 I.D.) 5.97 psi size questionable
8" (8.39 I.D.) 16.94 psi size ok
4~ ~~=0
12" (1165 I.D.) 1.62 psi size too large
10" (9.79 I.D.) 3.78 psi size questionable
$" (7.98 I.D.) 10.20 psi size ok
:'.E.
16" OC (13.090 I.D.) 0.93 psi size questionable
14" OD (11.454 I.D.) 1.77 psi size ok
12" OD (10.432 I.D.) 2.79 psi size ok
As the IO-inch DI, 10-inch PVC and 16-inch PE are questionable
s_ze pipes, it would appe ar that a 14-inch OD P.E. pipe wculd be
the most favorable for this situ ation. Pressure losses at various
flows through the 14-inch PE pipe for the 300-foot crossing length
would be:
1000 gpm 0.32 psi
2500 gpm 1.76 psi
3500 gpm 3.28 psi
5000 gpm 6.35 psi
As can be seen the pressure losses at the normal flows are very
minimal and for the extremely high fire flows are not excessive.
I-94 FRONTAGE ROAD WATERMAIN
The watermain would be placed on the north side of the frontage
.road, from the western end to across CSAH 37, see Attachment 2. It
;vould consist of approximately 2700 feet of 12-inch ductile iron
a I"•{R.,
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or FVG pipe. Hydrants would be placed in accordance with Joint
Powers' requirements. Services would be extended to the property
T lines for the lots along the frontage road. The CSAH 37 crossing
i wculd consist of approximately 70 feet of steel casing with a
" 12-inch. carrier. The casing and carrier would be jacked and bored
under the highway.
~~_o ;: s~p~l;'=,CE RCAD SPJ~ITARY SEWER
~~ __
~,:~e sanitary sewer would also be placed on the north side of the
;:ror_t,age road, from the western end to across CSAH 37, see
:attachment 2. It would consist of approximately 2700 feet of
i2-ir_ch PVC sewer pipe. Services would be extended to the property
li ~1Fs for the lots along the frontage road. The CSAH 37 crossing
r~oul:~ consist of approximately 80 feet of steel casing with a
12-inch PVC. carrier. The casing and carrier would be jacked and
bored under tine highway.
~iZe proposed invert elevation of the manhole at the western end of
the sanitary sewer would be approximately 942.5. The ordinary high
~:~ater (0?~w1) level of the lakes is 947.3. The lowest floor
elevation of any structure must be three feet above the OHW
elevation., resulting in a minimum floor elevation of 950.3.
fiherefore, the extent of gravity sanitary sewer into the area
between School and Mud Lakes would be dependent upon the plat
design, street grades, etc. This westerly line, however, would be
~he proposed outlet for any future upgrading of the forcemain from
_,
f;he ex~"sting lift station located in Sunrise Commercial Park, as
has been discussed by Council previously.
The proposed invert elevation at the easterly end of the sanitary
sewer line is approximately 943.5, which would service all of the
remaining developable property in Albertville above the wetland
elevation of approximately 950.0 feet.
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